Experimental combustion characteristics and NOx emissions for a 600-MWe utility boiler after the retrofitted: Effects of load variation

被引:1
|
作者
Wang, Haopeng [1 ]
Deng, Shanshan [1 ]
Ti, Shuguang [1 ,5 ]
Jin, Haoze [1 ]
Yang, Zhi [1 ]
Gao, Ke [1 ]
Wu, Xuehong [2 ]
Liu, Shengyong [3 ]
An, Jingxue [4 ]
Sheng, Ranran [4 ]
机构
[1] Zhengzhou Univ Light Ind, Coll Bldg Environm Engn, Zhengzhou, Peoples R China
[2] Zhengzhou Univ Light Ind, Coll Energy & Power Engn, Zhengzhou, Peoples R China
[3] Henan Agr Univ, Coll Mech & Elect Engn, Zhengzhou, Peoples R China
[4] China Datang Corp Sci & Technol Gen Res Inst Co Lt, Zhengzhou, Peoples R China
[5] Zhengzhou Univ Light Ind, Sch Bldg Environm Engn, Zhengzhou 450002, Peoples R China
关键词
air staging; load variation; NOx emissions; swirl burner; DOWN-FIRED BOILER; NUMERICAL-SIMULATION; SWIRL BURNER; FURNACE; FLOW;
D O I
10.1002/apj.3092
中图分类号
TQ [化学工业];
学科分类号
0817 ;
摘要
To enhance the rapid switching ability of the boiler load and reduce NOx emissions, a new combustion system was implemented in a 600-MWe wall-fired boiler with swirl burners. This system included two levels of overfire air (OFA) and low NOx combustion technology. Industrial tests were conducted at 300-, 450-, and 600-MWe loads before and after the retrofitted. These tests included measuring flue gas and furnace temperatures with thermocouples and analyzing local gas concentrations using a gas analyzer. The research results indicate that under conditions where the OFA ratio exceeds 30%, the burner exhibits good ignition performance at different loads. At the 600-MWe load, the nitrogen oxides (NOx) emissions were reduced by 55% compared to before the retrofit. After the retrofit, the flame center inside the furnace of different loads was located at the height of 33.36 m, the first and second-stage cooling water quantities were slightly higher, the reheat cooling water quantity was greatly reduced after the retrofit, and contributes to the boiler's safe operation. Under different load conditions after the retrofit, the gas temperature near the sidewall was below 850 degrees C, and the O-2 concentration near the sidewall was above 5%, effectively suppressing sidewall high-temperature corrosion and slagging.
引用
收藏
页数:10
相关论文
共 50 条
  • [21] Gas/Particle Flow Characteristics, Combustion and NOx Emissions of Down-Fired 600 MWe Supercritical Utility Boilers with Respect to Two Configurations of Combustion Systems
    Kuang, Min
    Li, Zhengqi
    Zhu, Qunyi
    Chen, Lizhe
    Zhang, Yan
    Lai, Jinping
    ENERGY & FUELS, 2012, 26 (06) : 3316 - 3328
  • [22] Overall Evaluation of Combustion and NOx Emissions for a Down-Fired 600 MWe Supercritical Boiler with Multiple Injection and Multiple Staging
    Kuang, Min
    Li, Zhengqi
    Liu, Chunlong
    Zhu, Qunyi
    ENVIRONMENTAL SCIENCE & TECHNOLOGY, 2013, 47 (09) : 4850 - 4858
  • [23] Industrial measurement of combustion and NOx formation characteristics on a low-grade coal-fired 600MWe FW down-fired boiler retrofitted with novel low-load stable combustion technology
    Du, He
    Li, Zhengqi
    Liu, Zheng
    Zhang, Mingdi
    Huang, Chunchao
    Jiang, Guangfei
    Chen, Zhichao
    Song, Jian
    Fang, Fan
    Su, Jianjun
    Liu, Haibing
    FUEL, 2022, 321
  • [24] Combustion characteristics and NOx emissions of two kinds of swirl burners in a 300-MWe wall-fired pulverized-coal utility boiler
    Li, Zhengqi
    Jing, Jianping
    Chen, Zhichao
    Ren, Feng
    Xu, Bin
    Wei, Hongda
    Ge, Zhihong
    COMBUSTION SCIENCE AND TECHNOLOGY, 2008, 180 (07) : 1370 - 1394
  • [25] Aerodynamic Characteristics of a 600-MWe Utility Boiler Incorporating Multi-Injection and Multi-Staging: Influences of the Distance between Adjacent Two Burners
    Song, Minhang
    Zeng, Lingyan
    Zhang, Shaofeng
    Zhao, Yan
    Pei, Jiangtao
    Zang, Xueli
    Li, Zhengqi
    COMBUSTION SCIENCE AND TECHNOLOGY, 2020, 192 (01) : 182 - 196
  • [26] Influence of the Parallel C-Layer Secondary Air on Flow, Combustion and Nox Generation Characteristics of a 600mwe FW Down-Fired Boiler Retrofitted with a Stable Combustion Organization Mode
    Du, He
    Li, Zhengqi
    Liu, Zheng
    Zhang, Mingdi
    Chen, Zhichao
    Song, Jian
    Fang, Fan
    Xiao, Ronghua
    COMBUSTION SCIENCE AND TECHNOLOGY, 2024, 196 (10) : 1529 - 1553
  • [27] Combustion and NOx emissions characteristics of a down-fired 660-MWe utility boiler retro-fitted with air-surrounding-fuel concept
    Ren, Feng
    Li, Zhengqi
    Liu, Guangkui
    Chen, Zhichao
    Zhu, Qunyi
    ENERGY, 2011, 36 (01) : 70 - 77
  • [28] Influence of Inner Secondary Air Vane Angle on Combustion Characteristics and NOx Emissions of a Down-Fired Pulverized-Coal 300 MWe Utility Boiler
    Fan, Subo
    Li, Zhengqi
    Zhu, Qunyi
    COMBUSTION SCIENCE AND TECHNOLOGY, 2013, 185 (06) : 975 - 989
  • [29] Issues in deep peak regulation for circulating fluidized bed combustion: Variation of NOx emissions with boiler load
    Ke, Xiwei
    Zhu, Shahong
    Huang, Zhong
    Zhang, Man
    Lyu, Junfu
    Yang, Hairui
    Zhou, Tuo
    ENVIRONMENTAL POLLUTION, 2023, 318
  • [30] Effect of the separated overfire air location on the combustion optimization and NOx reduction of a 600 MWe FW down-fired utility boiler with a novel combustion system
    Ma, Lun
    Fang, Qingyan
    Tan, Peng
    Zhang, Cheng
    Chen, Gang
    Lv, Dangzhen
    Duan, Xuenong
    Chen, Yiping
    APPLIED ENERGY, 2016, 180 : 104 - 115