Flexible and cost-effective optimization of BOG (boil-off gas) recondensation process at LNG receiving terminals

被引:44
|
作者
Li, Yajun [1 ]
Chen, Xingshui [1 ]
Chein, Ming-Hsiung
机构
[1] S China Univ Technol, Key Lab Heat Transfer Enhancement & Energy Conser, Minist Educ, Guangzhou, Guangdong, Peoples R China
来源
关键词
LNG; BOG; Recondenser; Compressor; Optimize; OPERATION;
D O I
10.1016/j.cherd.2012.01.013
中图分类号
TQ [化学工业];
学科分类号
0817 ;
摘要
In view of high energy consumption and poor flexibility in boil-off gas (BOG) recondensation operation at liquefied natural gas (LNG) terminals, a flexible and cost-effective optimization including the control system and flow process has been proposed. The optimized control system maintains BOG recondenser pressure via the condensing LNG flow and recondenser liquid level via bypass LNG flow. A BOG recondensation process with pre-cooling operation utilizes high-pressure pump LNG to pre-cool compressed BOG before it is directed into recondenser. The engineering application in a case of 6.69 tons/hour (t/h) BOG and LNG output fluctuating between 49 t/h and 562 t/h shows, after the flexible and cost-effective optimization, that process energy decreases 91.2 kW, more 1.28 t/h BOG is recovered when LNG output load reaches the valley, and the operation stability is well improved. (c) 2012 The Institution of Chemical Engineers. Published by Elsevier B.V. All rights reserved.
引用
收藏
页码:1500 / 1505
页数:6
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