Spillway radial gate failure at Folsom Dam, California

被引:0
|
作者
Todd, RV [1 ]
机构
[1] US Bur Reclamat, Denver Tech Serv Ctr, Mech Equipment Grp, Denver, CO 80225 USA
来源
DEALING WITH AGING DAMS | 1999年
关键词
D O I
暂无
中图分类号
TU [建筑科学];
学科分类号
0813 ;
摘要
On the morning of July 17, 1995, spillway radial gate No.3 failed at Folsom Dam, California. It was one of five service gates which had been operated by the Bureau of Reclamation since 1956. There was no warning of structural distress prior to the failure. No one was injured, even though there was a sustained release of 1,132 m(3)/s into the Lower American River. A multi-disciplinary, multi-agency forensic team was formed to investigate the failure. All of the remaining gates were thoroughly inspected for signs of structural degradation, apart from some corrosion, nothing detrimental was found. The failed gate was removed and then thoroughly examined to determine the mode of failure. This examination determined that a diagonal brace joint, adjacent to the trunnion was the initial point of failure. Theoretical finite element models substantiated this study when a trunnion friction coefficient of 0.25 was considered. This value had been confirmed also from friction tests performed on the actual trunnion from the failed gate. Trunnion friction moment was the key factor, and it had been omitted in the original design calculations.
引用
收藏
页码:15 / 29
页数:15
相关论文
共 50 条
  • [1] Folsom spillway gate failure and lessons learned
    Todd, RV
    ENERGY AND WATER: SUSTAINABLE DEVELOPMENT - PROCEEDINGS OF THEME D: WATER FOR A CHANGING GLOBAL COMMUNITY, 1997, : 66 - 71
  • [2] In-air and in-water natural vibrations of Folsom Dam radial gate in California
    Anami, K
    Ishii, N
    EXPERIMENTAL MECHANICS, VOLS 1 AND 2: ADVANCES IN DESIGN, TESTING AND ANALYSIS, 1998, : 29 - 34
  • [3] Folsom Dam spillway stilling basin repair
    Muller, BC
    Einhellig, RF
    WATER RESOURCES ENGINEERING 98, VOLS 1 AND 2, 1998, : 1511 - 1516
  • [4] Eliminating Vortices at the Proposed Folsom Dam Auxiliary Spillway
    Barfuss, Steven L.
    Rahmeyer, William J.
    Cox, Nathan C.
    ADVANCES IN HYDRAULIC PHYSICAL MODELING AND FIELD INVESTMENT AND INVESTIGATION, 2010, : 413 - 420
  • [5] California Division of Safety of Dams spillway radial gate program
    Gutierrez, DA
    Sage, FJ
    ASSOCIATION OF STATE DAM SAFETY OFFICIALS 1998 ANNUAL CONFERENCE PROCEEDINGS, 1998, : 491 - 499
  • [6] Flow-induced dynamic instability closely related to Folsom Dam Tainter-Gate failure in California
    Anami, K
    Ishii, N
    FLOW-INDUCED VIBRATION, 2000, : 205 - 212
  • [7] Insights into the cause of the Oroville dam spillway failure, 2017, California
    Xingsheng Zhang
    Chaoyue Wang
    Xing Chen
    Jinyu Dong
    Mengke Hu
    Shipeng Liu
    Environmental Science and Pollution Research, 2024, 31 : 21356 - 21369
  • [8] Insights into the cause of the Oroville dam spillway failure, 2017, California
    Zhang, Xingsheng
    Wang, Chaoyue
    Chen, Xing
    Dong, Jinyu
    Hu, Mengke
    Liu, Shipeng
    ENVIRONMENTAL SCIENCE AND POLLUTION RESEARCH, 2024, 31 (14) : 21356 - 21369
  • [9] Work Begins on Control Structure for Folsom Dam Auxiliary Spillway
    Landers, Jay
    CIVIL ENGINEERING, 2011, 81 (03): : 34 - 35
  • [10] FOUNDATION PROBLEMS, FOLSOM DAM PROJECT, CALIFORNIA
    TREASHER, RC
    ROSE, MF
    GEOLOGICAL SOCIETY OF AMERICA BULLETIN, 1951, 62 (12) : 1513 - 1514