A new integrated approach of coal gasification: the concept and preliminary experimental results

被引:13
|
作者
Wu, JH [1 ]
Fang, YT [1 ]
Peng, H [1 ]
Wang, Y [1 ]
机构
[1] Chinese Acad Sci, Inst Coal Chem, Taiyuan 030001, Peoples R China
关键词
integrated; coal gasification; fluidized bed; entrained flow;
D O I
10.1016/j.fuproc.2004.03.005
中图分类号
O69 [应用化学];
学科分类号
081704 ;
摘要
The total carbon conversion of conventional fluidized bed gasifier is relatively low (<90%) mainly because of carbon loss in fly-ash. In this paper, a new concept of integrated coal gasification-fluidized bed+entrained flow is introduced. Within this process, large partition of coal with higher reactivity is converted in an ash agglomerating fluidized bed reactor under moderate temperature (similar to1000 degreesC). The remaining small partition of coal (fly-ash) with lower reactivity is converted in a small integrated entrained flow gasifier under higher temperature (1200-1400 degreesC). Low carbon content ash is withdrawn in dry mode by ash agglomerating, with no need to be melted. Preliminary experimental results show that the whole system can be operated steadily, total carbon conversion reaches >95%, efficient gas (CO+H-2) concentration is 78-82%. Heat exchange between two reactors has been realized, the high temperature gas from entrained flow gasifier can be cooled, and in the mean time the temperature of fluidized bed nearly keeps constant. The high-temperature ash from entrained flow gasifier can be cooled by the char in dense phase of the fluidized bed and then withdrawn in agglomerating mode. All these results prove the concept correct and feasible. (C) 2004 Elsevier B.V. All rights reserved.
引用
收藏
页码:261 / 266
页数:6
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