Experimental Investigation of an Aerodynamically Mistuned Oscillating Compressor Cascade

被引:12
|
作者
Malzacher, Leonie [1 ]
Schwarze, Christopher [1 ,2 ]
Motta, Valentina [1 ]
Peitsch, Dieter [1 ]
机构
[1] Tech Univ Berlin, Dept Aeronaut & Astronaut, Marchstr 12-14, D-10587 Berlin, Germany
[2] Lufthansa Tech AG, Weg Beim Jager 193, D-22335 Hamburg, Germany
来源
关键词
FLUTTER;
D O I
10.1115/1.4043474
中图分类号
TH [机械、仪表工业];
学科分类号
0802 ;
摘要
In this paper, the effect of aerodynamic mistuning on stability of a compressor cascade is studied. The experiments have been carried out at a low-speed test facility of the Technische Universitat Berlin. The test section contains a linear cascade with compressor blades that are forced to oscillate in sinusoidal pitching motion. The aerodynamic mistuning is realized by a blade-to-blade stagger angle variation, and three mistuning patterns have been investigated: one-blade mis-staggering, alternating mis-staggering, and random mis-staggering. Mis-staggering can have a stabilizing or destsabilizing effect, but depends strongly on the amount of detuning that alters the flow passage. For positive stagger angle variation for the one-blade and alternating mis-staggering, the trend of the damping curve was maintained, in the sense that the unstable interblade phase angles (IBPAs) remained unstable. For negative stagger angle variation, one IBPA shifted from stable to unstable. For the random pattern, only very moderate changes are observed. The cascade stability was not noticeably affected by the aerodynamic mistuning.
引用
收藏
页数:9
相关论文
共 50 条
  • [41] EXPERIMENTAL INVESTIGATION OF EFFECTS OF LEADING-EDGE TUBERCLES ON COMPRESSOR CASCADE PERFORMANCE
    Keerthi, M. C.
    Kushari, Abhijit
    De, Ashoke
    Kumar, Arun
    PROCEEDINGS OF THE ASME TURBO EXPO: TURBINE TECHNICAL CONFERENCE AND EXPOSITION, 2014, VOL 2A, 2014,
  • [42] EXPERIMENTAL AND NUMERICAL INVESTIGATION OF CORNER STALL IN A HIGHLY-LOADED COMPRESSOR CASCADE
    Zhang, Yanfeng
    Mahallati, Ali
    Benner, Michael
    PROCEEDINGS OF THE ASME TURBO EXPO: TURBINE TECHNICAL CONFERENCE AND EXPOSITION, 2014, VOL 2A, 2014,
  • [43] Experimental and numerical investigation of the unsteady tip leakage flow in axial compressor cascade
    Chengqing Li
    Tingfeng Ke
    Jingxuan Zhang
    Hongwu Zhang
    Weiguang Huang
    Journal of Thermal Science, 2013, 22 : 103 - 110
  • [44] Experimental and numerical investigation for flow in bowed compressor cascade with large turning angles
    School of Energy Science and Engineering, Harbin Inst. of Technology, Harbin 150001, China
    不详
    Tuijin Jishu, 2008, 3 (349-354):
  • [45] Experimental investigation on separation control by slot jet in highly loaded compressor cascade
    Hu Jiaguo
    Wang Rugen
    Li Renkang
    He Chen
    Li Qiushi
    PROCEEDINGS OF THE INSTITUTION OF MECHANICAL ENGINEERS PART G-JOURNAL OF AEROSPACE ENGINEERING, 2018, 232 (09) : 1704 - 1714
  • [46] EXPERIMENTAL INVESTIGATION ON TIP CLEARANCE FLOW OF COMPRESSOR CASCADE WITH BLADE TIP WINGLET
    Han, Shaobing
    Zhong, Jingjun
    Lu, Huawei
    Kan, Xiaoxu
    Gao, Haiyang
    PROCEEDINGS OF THE ASME TURBO EXPO 2012, VOL 8, PTS A-C, 2012, : 353 - 360
  • [47] NUMERICAL AND EXPERIMENTAL INVESTIGATION ON A LOW-SPEED COMPRESSOR CASCADE WITH CIRCULATION CONTROL
    Fischer, S.
    Saathoff, H.
    Radespiel, R.
    PROCEEDINGS OF THE ASME TURBO EXPO 2008, VOL 6, PT A, 2008, : 219 - 228
  • [48] Experimental and Numerical Investigation of the Unsteady Tip Leakage Flow in Axial Compressor Cascade
    Chengqing Li
    Tingfeng Ke
    Jingxuan Zhang
    Hongwu Zhang
    Weiguang Huang
    Journal of Thermal Science, 2013, 22 (02) : 103 - 110
  • [49] Compressible Modal Instability Onset in an Aerodynamically Mistuned Transonic Fan
    Brandstetter, Christoph
    Paoletti, Benoit
    Ottavy, Xavier
    JOURNAL OF TURBOMACHINERY-TRANSACTIONS OF THE ASME, 2019, 141 (03):
  • [50] SIMULATION AND INVESTIGATION OF AN INTENTIONALLY MISTUNED BLISK ROTOR IN A HIGH PRESSURE COMPRESSOR
    Yang, Jingjie
    Beirow, Bernd
    Giersch, Thomas
    PROCEEDINGS OF ASME TURBO EXPO 2022: TURBOMACHINERY TECHNICAL CONFERENCE AND EXPOSITION, GT2022, VOL 8B, 2022,