Failure of a Squeeze-Clamped Polyethylene Natural Gas Pipeline

被引:0
|
作者
Jones, Robert E., Jr. [1 ]
Bradley, Walter L. [2 ]
机构
[1] Univ Texas San Antonio, San Antonio, TX 78249 USA
[2] Texas A&M Univ, College Stn, TX USA
关键词
Clamping damage; Mechanical properties; Natural gas pipes; Plastic pipe; Residual stress; Stable crack propagation; High-density polyethylene; Ductile fracture;
D O I
10.1007/s11668-022-01515-5
中图分类号
T [工业技术];
学科分类号
08 ;
摘要
A high-density polyethylene (HDPE) natural gas distribution pipe (Grade PE 3306) failed by slow, stable crack growth while in residential service. The leak occurred at a location where a squeeze clamp had been used to close the pipe during maintenance. Failure analysis showed that the origin of the failure was a small surface crack in the inner pipe wall produced by the clamping. Fracture mechanics calculations confirmed that the suspected failure process would result in a failure time close to the actual time to failure. It was recommended that: materials be screened for susceptibility to the formation of the inner wall cracks since it was not found to occur in pipe typical of that currently being placed in service; pipes be re-rounded after clamp removal to minimize residual stresses which caused failure; and a metal reinforcing collar be placed around the squeeze location after clamp removal.
引用
收藏
页码:2023 / 2029
页数:7
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