Failure Analysis of Rubbing of the Fan Tip and Case of an Engine

被引:3
|
作者
Wei Feifei [1 ]
Chen Yunyong [1 ]
Wu Zhiqing [1 ]
Chen Lulu [1 ]
Meng Jin [1 ]
机构
[1] AVIC COMMER AIRCRAFT ENGINE CO LTD, R&D Ctr, Dept Compress Syst, Shanghai 201108, Peoples R China
关键词
Performance test; Hard rubbing of the fan tip and case; Failure analysis; Test verification;
D O I
10.1016/j.proeng.2014.12.661
中图分类号
V [航空、航天];
学科分类号
08 ; 0825 ;
摘要
Unexpected hard rubbing of the fan tip and case occurred during the reduced-scale high-bypass fan performance test which took place at a bypass compressor Test-Facility of an institute. A great deal of effort had been expended with regard to this event. Firstly, failure investigation was done by means of Fault Tree Analysis which was based on the on-site test failure records, test pieces dis-assembly check and Test-Facility check. Results indicate that the fault was possibly caused by the combination effect of over-rated motor starting acceleration and insufficient value of the fan blade tip clearance and axial length of the case coating in design. Then, failure reproduction, confirmation of reasons and mechanism analysis were done by simulating the spinner cone bolt deformation and simulating the rubbing of fan blades and case, in combination with the analysis of the characteristics of fan blade and the no-load test of motor starting. Finally, in order to solve the problem, several improvements were established, including modifying the motor speed limit parameters to reduce the starting acceleration, increasing the fan blade tip clearance and increasing the axial length of the case coating. These solutions were verified by test. (C) 2015 Published by Elsevier Ltd.
引用
收藏
页码:1289 / 1296
页数:8
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