Mobile pilot plant for CO2 capture in biogas upgrading using 30 wt% MEA

被引:6
|
作者
Jorsboe, Jens Kristian [1 ]
Vinjarapu, Sai Hema Bhavya [1 ]
Neerup, Randi [1 ]
Moller, Andreas Christian [1 ]
Jensen, Soren [2 ]
Abildskov, Jens [3 ]
Fosbol, Philip [1 ]
机构
[1] Tech Univ Denmark, Ctr Energy Resource Engn CERE, Soltofts Plads 228A, DK-2800 Lyngby, Denmark
[2] Pentair Union Engn AS, Snaremosevej 27, DK-7000 Fredericia, Denmark
[3] Tech Univ Denmark, Prosys, Soltofts Plads 228A, DK-2800 Lyngby, Denmark
关键词
Carbon capture; Biogas upgrading; Amine scrubbing; Monoethanolamine; Pilot; -scale; Mobile plant; CARBON-DIOXIDE; ABSORPTION; DENSITY; GAS;
D O I
10.1016/j.fuel.2023.128702
中图分类号
TE [石油、天然气工业]; TK [能源与动力工程];
学科分类号
0807 ; 0820 ;
摘要
This study utilizes a new mobile pilot plant to capture CO2 from real biogas with 30 wt% monoethanolamine (MEA). The pilot plant is described in detail and validated by data reconciliation showing that the pilot plant produces reliable steady state data. It is demonstrated that the pilot plant can upgrade 32 kg biogas per hour by capturing 20 kg CO2 per hour. Further, the pilot plant can achieve below 2.5 mol% CO2 in the methane product at a specific reboiler duty of 3.74 GJ per ton of CO2. The absorber column was found to be operated close to pinch conditions as temperatures reached above 90 degrees C giving a potential for process optimization and heat integration.
引用
收藏
页数:12
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