Optimization and Performance Evaluation of Foam Discharge Agent for Deep Aquatic Condensate Gas Well

被引:0
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作者
Ge, Lei [1 ]
Cui, Hailin [2 ]
Li, Yingchao [3 ]
Sui, Xiuan [3 ]
机构
[1] Sinopec Shengli Petroleum Engineering Company Limited Tarim Branch, Kuerle, China
[2] Drilling Technology Research Institute of Sinopec Shengli Oilfield Service Corporation, Dongying, China
[3] School of Petroleum Engineering, China University of Petroleum, Qingdao, China
关键词
Gas condensates - Gases - Injection (oil wells) - Petroleum reservoirs - Two phase flow - Wellheads;
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学科分类号
摘要
The block deep condensate gas reservoir in the basin in the southeast of the South China Sea is a bottom water reservoir and is producing in the late effusion, which faces problems such as scaling, condensate oil–water two-phase flow, and low temperature at the subsea wellhead. The mud line for this kind of gas-well has characteristics including high condensate content in low temperature, high downhole temperature, and injection with a foam discharge agent and scale inhibitor. In this article, the influence of low temperature and scale inhibitor is considered for the first time, and a dynamic liquid-carrying experiment for the optimization and performance evaluation of foam discharge agents was carried out according to these characteristics. The experimental results show that the optimized foam discharge agent, ZHY-01, has good resistance to high temperature and condensate oil, and the optimal concentration of the foam discharge agent is recommended to be 0.25%. Under this concentration, the liquid-carrying capacity of the foam discharge agent decreases slightly by 10.17% at low temperature. The scale inhibitor MA/AA reduced the liquid-carrying capacity by 11.86%, and the scale inhibitor PESA reduced the liquid-carrying capacity by 10.17%. The research results in this article have certain reference significance for the chemical screening and evaluation of the foam drainage gas production process in deep-water condensate gas wells. Copyright © 2022 Ge, Cui, Li and Sui.
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