A case study on causes and countermeasures of a largely deformed geotextile-reinforced soil retaining wall

被引:0
|
作者
Hur, Jinsuk [1 ]
Jung, Minsu [2 ]
Shibuya, Satoru [1 ]
机构
[1] Kobe Univ, Dept Civil Engn, Kobe, Hyogo, Japan
[2] Korea Inst Construct Technol, Goyang Si, South Korea
关键词
geotextile; reinforced soil retaining wall; site investigation; laboratory test; numerical analysis;
D O I
10.3233/978-1-60750-822-9-1268
中图分类号
P5 [地质学];
学科分类号
0709 ; 081803 ;
摘要
The horizontal displacement more than 16cm occurred on the facing of a 20m high reinforced soil retaining wall that was under construction for the purpose of the alignment improvement of the existing national highway located in Hyogo, Japan. In this paper, the causes of the excessive deformation, together with the numerical examination into countermeasures are in detail described. First, various site investigations and laboratory tests were carried out to manifest the current state of the reinforced soil retaining wall. Second, the deformation behavior of the wall was simulated by performing numerical analysis. Finally, an appropriate countermeasure to prevent further development of the wall deformation was proposed by predicting the stress-strain behavior of the reinforced soil retaining wall with the remedial work.
引用
收藏
页码:1268 / 1275
页数:8
相关论文
共 50 条