Failure analysis on the oxygen corrosion of the perforated screens used in a gas injection huff and puff well

被引:3
|
作者
Fan, Lei [1 ]
Gao, Yuan [1 ,2 ]
Yuan, Juntao [1 ]
Yin, Chenxian [1 ]
Fu, Anqing [1 ]
Zhao, Mifeng [3 ]
Li, Yan [3 ]
Suo, Tao [4 ]
Du, Xiaoyi [4 ]
Wang, Yanhai [4 ]
机构
[1] CNPC Tubular Goods Res Inst, State Key Lab Performance & Struct Safety Petr Tu, Xian 710077, Shaanxi, Peoples R China
[2] Xian Univ Architecture & Technol, Sch Chem & Chem Engn, Xian 710055, Peoples R China
[3] Petro China Tra Oilfield Co, Korla 841000, Peoples R China
[4] Petrochina Changqing Petrochem Co, Xianyang 712042, Shaanxi, Peoples R China
基金
美国国家科学基金会;
关键词
Gas injection and puff well; Nitrogen; Corrosion; Failure analysis; Oxygen corrosion;
D O I
10.1016/j.engfailanal.2020.104984
中图分类号
TH [机械、仪表工业];
学科分类号
0802 ;
摘要
The perforated screens of a gas injection huff and puff well broke down in an oilfield in western China. The physical and chemical properties of the failure-perforated screens met the requirements of relevant technical protocols. The injected gas was nitrogen produced by the membrane nitrogen method, which contains approximately 5% O-2. Therefore, a substantial amount of O-2 entered the well during the gas injection, and greatly promoteed the cathodic process of the electrochemical corrosion. High salinity formation water, especially with large amounts of Cl-, further accelerated the corrosion. The significant oxygen corrosion under the well finally led to the failure of the perforated screen.
引用
收藏
页数:8
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